Monday, 29 August 2011

Pershore Plum Festival 2011

Set off at 8 and met up with Pete for the latest Beast adventure, this time to the Pershore car and plum and hippy stuff festival. After meeting up with Mike, Sheila and Paul, we got onto the field at about 9. Here is a crap picture of the 5 cars...

The fields soon filled up with loads of makes and models of cars and billions of people gawping at the pretty cars whilst chomping their plums, ice creams and pork roils.

And the Beast? Behaved perfectly.How I ever doubted my little car! MOT due soon mind...

Saturday, 6 August 2011

Sunday 31st July

The 12th Malvern Classic Car Show and Classic Ford Day (including Capripower National Day  at the Three Counties Showground, Malvern) is today. I picked up Simon (to navigate/mechanic/push/amuse me) and we then met Pete (TRDC) at the Rose and Crown in Stourport. 

The temp gauge is already at half. But I am not putting the fans on, I want to see what happens. We "zoom" off up the Worcester Road A449 towards the motorway. The Beast has now done the longest journey sine I had it 3+ years ago! After a junction of the M5, we pull in and wait for the rest of the TRDC. It's very hot, so the fans now go on, which is just as well as the Worcester bypass to Malvern road thing is always packed. We sat for ages and ages and I was fully expecting the Beast to explode, but no, it soldiered on.

By the turning to Malvern, the traffic became even denser due to a blonde chick breaking down in a crappy Ford Ka. It was at this point that I tempted fate, turning to my co-driver and suggesting she ought to have bought a reliable Triumph instead. I then managed to stall. And it wouldn't start again. Simon pushed, and I managed to bump it. Off we continued to the showground.

When we got there, we had a look around the piles of rusty crap/stalls and a few of the other cars. I then asked old Mike (TRDC) if he could help me put the bonnet scoop/fresh air thingy back on as I hadn't managed to get the bugger on. "Never mind that. What's happened here?". Oh F*ck. I hadn't filled the dashpots nor put the pistons back in, hence the earlier picture. They looked as good as new after they had been (almost) straightened with a trolley jack handle and a pair of pliers! And Mike and Rich even managed to put the bonnet scoop/fresh air thingy back on.

The  return journey was uneventful. I now have faith in the Beast to take me on any (short) journey. I now even go home from work (when sunny) the long way. The temp gauge still sits nicely on half.

Saturday 30th July

The 12th Malvern Classic Car Show and Classic Ford Day (including Capripower National Day  at the Three Counties Showground, Malvern) is tomorrow, so I gave the Beast a good clean, polish, wax, hoover. I also stupidly opened the bonnet. I really shouldn't be allowed under there.
 I topped up the water and oil and unscrewed the carb damper pistons from the carbs and went to get some oil. Which I didn't get as my memory is going. I returned and closed the bonnet. And put the Beast back in the Beastport.

Tuesday, 21 June 2011

June

The Beast has been used regularly over the last few weeks, whenever there has been a non-rainy weekday. It even managed the long journey to Stourport (!) to the June TRDC meeting for the first time! It's still overheating according to the temp gauge but has yet to go bang. The only slight problem was on the way back from work on 20th June where the engine simply died. I even managed to fix it myself - a wire had fallen off the coil! So far still so good ...

Tuesday, 24 May 2011

Still going

It's still going! I have brought it in again today, after a week of idleness due to May's April showers. Typically there are still lots of problems, ie, the centre console lid fell off this morning! I will need to do another "To Do List" soon. I may even try to get out of Kidderminster before the MOT runs out in September!

This post was actually a couple of weeks ago, but I have just edited it and now the date stamp has changed! Anyway, assuming I get back in one peice from picking Moo up from Guides, I shall be taking it in tomorrow too! Still not gone outside the Kidderminster town barriers yet ...

Tuesday, 19 April 2011

Toyota Celica - Pah!

Why would I want one of them Japanese pretend classics when I have a fully working [well sort of] v8 Beast?! 

It would appear that the distributor was 180 degrees out. And with the assistance of Simon and Ed's timing strobe, the Beast spluttered into life and is now running the best it ever has in the last 3 years. Much also say thanks to a chap named John in Aberdeen with whom I have been conversing via email and a v8 forum.

That distributor is the dogs! We timed it to about 8 dibbles past TDC. Although it is now driveable, it "front fires" from I presume the carbs/filters as opposed to backfiring from the tailpipe. I have taken it to work for the last 2 days and can (sometimes) floor it without any frontfires and now get the great v8 roar. 

I have since spoken to John again, who has set his distributor at 10 dibbles before TDC. He reckons that the frontfiring is because the timing is not quite right, and suggests I try it at 10 dibbles.

The overheating thing has still not gone away though. Could it be the timing? The gauge?

Wednesday, 13 April 2011

March and April

Pre new Distributor
I have been driving around Offmore every other Sunday for about 5 mins before putting it back again as it was spluttering and backfiring and overheating. I was a little brave the one day though and sat in the car port with the temp guage at 3/4 waiting for it to blow up. It didn't. Looks like 3/4 might be the running temperature?

Post new Distributor
It doesn't start any more!